Re: Nick's VVC tidyup
Posted: Fri Apr 27, 2018 3:55 pm
I've been nibbling away at the welding the MOT tester required, which included replacing the entire lower rear valence and where it wraps round into the wheelarches; attaching the previously 'repaired' NSR wheel arch to the inner structure(it wasn't attached to ANY of it
), redoing a similar budgie shit where it touches repair on the NSR wheeltub, both floors in front of the rear jacking points, and the chassis rail behind the OSF anti-rollbar mount. Plenty of seam sealer in the joints and a thick coating of schutz, and none of it looks too bad.
On starting the car to take it to the MOT this morning, I discovered it had NO brakes. Which required a grovel at the garage(only 100m down the road) and a quick fit of the new master cylinder I bought when I got the car. Then I found that I'd used most of my brake fluid fitting bigger brakes to a mates MGF last week, so that all took longer than I expected.
They had another space this afternoon for the MOT, and after I fitted two new wiper blades - it only needed one but I swapped the better one to the back - and a new headlight bulb which was working but giving a poor beam pattern, it passed
I'm pleasantly surprised by the Sportex exhaust; I was expecting it to sound like a cow farting down a drainpipe, instead it has a decent burble and isn't too loud. I hate loud cars. The road noise that was coming in through the massive gaps in the car's structure is now much quieter.
That just leaves the coolant leak to fix with the correct sized clamp in the morning and the car ought to be usable again. I do need to rewire the manually switched cooling fan back to the proper temperature switch though.

On starting the car to take it to the MOT this morning, I discovered it had NO brakes. Which required a grovel at the garage(only 100m down the road) and a quick fit of the new master cylinder I bought when I got the car. Then I found that I'd used most of my brake fluid fitting bigger brakes to a mates MGF last week, so that all took longer than I expected.
They had another space this afternoon for the MOT, and after I fitted two new wiper blades - it only needed one but I swapped the better one to the back - and a new headlight bulb which was working but giving a poor beam pattern, it passed

I'm pleasantly surprised by the Sportex exhaust; I was expecting it to sound like a cow farting down a drainpipe, instead it has a decent burble and isn't too loud. I hate loud cars. The road noise that was coming in through the massive gaps in the car's structure is now much quieter.
That just leaves the coolant leak to fix with the correct sized clamp in the morning and the car ought to be usable again. I do need to rewire the manually switched cooling fan back to the proper temperature switch though.